深圳抽水蓄能电站水力劈裂试验研究

艾凯, 刘元坤, 韩晓玉

长江科学院院报 ›› 2008, Vol. 25 ›› Issue (5) : 46-49.

PDF(267 KB)
PDF(267 KB)
长江科学院院报 ›› 2008, Vol. 25 ›› Issue (5) : 46-49.
水工岩石力学会议专辑

深圳抽水蓄能电站水力劈裂试验研究

  •  艾凯, 刘元坤, 韩晓玉
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Research of Hydrojacking Tests at Shenzhen Pumped Storage Power Plant

  •  AI  Kai, LIU  Yuan-Kun, HAN  Xiao-Yu-
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摘要

深圳抽水蓄能电站高压岔管区洞室内水压力高,为论证深圳抽水蓄能电站高压岔管区采用钢筋混凝土衬砌的可行性,进行了现场水力劈裂试验,测试裂隙岩体的抗劈裂能力和相应的P-Q曲线。试验结果表明:岔管围岩的劈裂压力大于1.2倍的内水压力。因此在做好防渗设计的基础上,采用钢筋混凝土衬砌方案是可行的。

Abstract

In order to verify the feasibility of reinforced concrete lining at the high pressure turnout of? Shenzhen Pumped Storage Power Plant, a field investigation of hydrojacking was done at site. Test results and P-Q curves show that the jacking pressure of surrounding rockmass is 1.2 times higher than internal water pressure. Therefore, on the basis of the effective anti-seepage design adopted, the reinforced concrete lining at the high pressure branch is feasible.

关键词

抽水蓄能电站 / 水力劈裂 / 裂隙 / P-Q曲线

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艾凯, 刘元坤, 韩晓玉. 深圳抽水蓄能电站水力劈裂试验研究[J]. 长江科学院院报. 2008, 25(5): 46-49
AI Kai, LIU Yuan-Kun, HAN Xiao-Yu-. Research of Hydrojacking Tests at Shenzhen Pumped Storage Power Plant[J]. Journal of Changjiang River Scientific Research Institute. 2008, 25(5): 46-49

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